1992-1999 Series I L27 (1992-1994 SE,SLE, SSE) & Series II L36 (1995-1999 SE, SSE, SLE) and common problems for the Series I and II L67 (all supercharged models 92-99) Including Olds 88's, Olds LSS's and Buick Lesabres Please use General Chat for non-mechanical issues, and Performance and Brainstorming for improvements.

Dorman UIM Interference Fit & Update to my 98 Project

Old May 3, 2006 | 10:37 PM
  #1  
trickytransam's Avatar
Thread Starter
Junior Member
Posts like a V-Tak
 
Joined: Apr 2006
Posts: 27
Likes: 0
trickytransam is on a distinguished road
Default Dorman UIM Interference Fit & Update to my 98 Project

The saga continues..

I wanted to post a blurb to the members, in case someone has the same issue that I had with the new Dorman Upper Intake.

Here is a link to my Myspace page, and check out the 3800 Series II Explosion picture gallery, which was recently updated to show the new Intake, Smaller EGR Tube and etc.
http://spaces.msn.com/trickytransam/

After going into surgery to replace the lower intake gaskets, I was buttoning up the whole top half of the motor.
I went to put on the alternator, and there was an interference fit on the corner of the NEW Dorman manifold. (615-180)

The Old Manifold was a Napa "Improved" - which I believed to be a dorman as it was Made in Korea, and had a Flat LIP on the corner.
The New Dorman Manifold had a large reinforced corner that the alternator housing contacted, and would not go into place. Made in the USA (Figures they wouldn't check for fit)

I had to grind out the corner where it was hitting, as I could NOT take the manifold back to AutoZone after it had been bolted down. (Plus I wanted this piece of crap out of my garage)

Anyone else have this interference problem?

Also, just an update on my other threads - Vacuum in the crankcase went Bye Bye after LIM were replaced, and along with it, the Vibrating PCV Valve.
180 Deg Thermostat installed with the Tranny cooler, and the Machined down solid stock tube. This was a tight press fit, that I locktited into place, and sits BELOW the gasket. Tube ID is 1/2". Seems to work perfectly so far.....
Car runs good, but still has really poor Oiling at lower RPM'*. Idle after driving, the oil pressure drops into the 20'*. While driving, its around 40-50 psi.
The other issue is that Cylinder #4 is at 120 psi during a compression check, and all the rest are around 165psi. One Flyer at 172, but it'* still within the 70% the manual is calling out.
Sad for an engine that only has 11K miles on it....

Hope this helps someone out.
Reply
Old May 4, 2006 | 08:00 AM
  #2  
BillBoost37's Avatar
DINOSAURUS BOOSTUS

Expert Gearhead
 
Joined: Mar 2005
Posts: 41,391
Likes: 30
From: Enfield, CT
BillBoost37 is a glorious beacon of lightBillBoost37 is a glorious beacon of lightBillBoost37 is a glorious beacon of lightBillBoost37 is a glorious beacon of lightBillBoost37 is a glorious beacon of lightBillBoost37 is a glorious beacon of light
Default

I haven't heard of any problems. Can you get some better pictures. It is very tough to see the actual issue in your pic.
Reply
Old May 4, 2006 | 05:20 PM
  #3  
trickytransam's Avatar
Thread Starter
Junior Member
Posts like a V-Tak
 
Joined: Apr 2006
Posts: 27
Likes: 0
trickytransam is on a distinguished road
Default

Well the car'* in detroit now. The pic is near the PCV valve side, and the interference is where the alternator housing bolt is.
Reply
Old May 5, 2006 | 07:47 PM
  #4  
Bob Dillon's Avatar
Senior Member
Posts like a Camaro
 
Joined: Feb 2005
Posts: 922
Likes: 8
From: Gilroy, California
Bob Dillon is on a distinguished road
Default

How much had to be ground off?
Reply
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
Maymybonnieliveforevr
Lounge
6
May 2, 2007 06:07 PM
bill buttermore
1992-1999
9
Feb 13, 2007 11:00 AM
Woody_02SilverSE
2000-2005
19
Nov 3, 2006 07:38 AM
jmandeville
1992-1999
22
Feb 20, 2006 04:08 PM
kcjones
1992-1999
6
Jan 27, 2006 05:33 PM


Thread Tools
Search this Thread

All times are GMT -4. The time now is 09:58 PM.