Low boost due to porting??
i have a 94 ssei
i just rebuilt the entire motor, gasket matched the heads to the intake and the ported exhaust manifolds, i also ported the intake extensivly , before i rebuilt it, i ran about 10psi but now i only get 7-8.5 (autometerprocomp guage) and i even have a 2.5" pulley on it
i have a aem wideband which reads 11.0 with my meth on
i scan my car everytime i drive it and i have 0 kr and about 18 degrees of timing advance
any help would be great
thanks
i just rebuilt the entire motor, gasket matched the heads to the intake and the ported exhaust manifolds, i also ported the intake extensivly , before i rebuilt it, i ran about 10psi but now i only get 7-8.5 (autometerprocomp guage) and i even have a 2.5" pulley on it
i have a aem wideband which reads 11.0 with my meth on
i scan my car everytime i drive it and i have 0 kr and about 18 degrees of timing advance
any help would be great
thanks
If you really GASKET matched, your port velocity may be suffering. While I agree with the loss of boost reasons stated above, you may have over-ported. I'd strongly suggest a cam or higher ratio rockers at this point.
i actually ported to one sharpe line or 1/16 to the inside, sos not to get carried away,
i put my other pulley on its a 2.1" from pulley boys and tuned with my afc and my air/ fuel is at 10.9- 11.3 with 18 degrees of advance , 0 knock retard, and my blower only still puts out 10-11 psi
the performance is great the power is right there all the time but the low boost numbers still have me concerned
thanks again
i put my other pulley on its a 2.1" from pulley boys and tuned with my afc and my air/ fuel is at 10.9- 11.3 with 18 degrees of advance , 0 knock retard, and my blower only still puts out 10-11 psi
the performance is great the power is right there all the time but the low boost numbers still have me concerned
thanks again
actally i have lots of stuff done to the motor
complete underdrive pulley kit - custom made
160 degree t-stat
custom ordered bosch 38lb injectors
ported intake
ported heads
ported exhaust manifolds, lots of material removed
no cat
hi flow dual outlet exhaust
fenderwell intake
auto lite 103 plugs gapped at 45 (copper)
egr removed and tuned out of the computer via custom chip
custom boost controller
water/ meth injection, custom controller
and a 4t65e hd with a 2750 stall converter and a stage 3 shift kit
complete underdrive pulley kit - custom made
160 degree t-stat
custom ordered bosch 38lb injectors
ported intake
ported heads
ported exhaust manifolds, lots of material removed
no cat
hi flow dual outlet exhaust
fenderwell intake
auto lite 103 plugs gapped at 45 (copper)
egr removed and tuned out of the computer via custom chip
custom boost controller
water/ meth injection, custom controller
and a 4t65e hd with a 2750 stall converter and a stage 3 shift kit
You swapped in a 4T65E? Interesting. Hows the computer like that? Did you rewire the tranny? I thought they had different wiring.
Sorry, that'* off topic. Start a new thread if you want to discuss the changes you did to the tranny.
Sorry, that'* off topic. Start a new thread if you want to discuss the changes you did to the tranny.



