1992-1999 Series I L27 (1992-1994 SE,SLE, SSE) & Series II L36 (1995-1999 SE, SSE, SLE) and common problems for the Series I and II L67 (all supercharged models 92-99) Including Olds 88's, Olds LSS's and Buick Lesabres Please use General Chat for non-mechanical issues, and Performance and Brainstorming for improvements.

Trans going into Gear problem. *Update - Video *

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Old 12-20-2006, 06:57 PM
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Any foaming or bubbles in the fluid?
Old 12-20-2006, 06:57 PM
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Originally Posted by Archon
Any foaming or bubbles in the fluid?
nope, it a nice Red with a hint of Brown still cuz its only 1/2 clean now
Old 12-20-2006, 07:06 PM
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If you think that something is gunked up (technical term ) you can try a can of Seafoam'* TransTune and see if it frees it up. It worked on my daughter'* tranny when it was slipping while cold. I used it at the suggestion of a mechanic who recommended it. Other than that, you may have to remove those thousands of bolts again and drop the pan to see if maybe the filter developed a crack.
Old 12-20-2006, 07:52 PM
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Originally Posted by jr's3800
Originally Posted by bandit
I used the old sleeve because i could not find a way to take that old one out safely.
And the new one wasn't even on the new filter.
If i though i could have gotten the old one out with out screwing my self with getting it stuck then i would have. Cuz it was in there pretty good.

Far as how tight the new filter went in, it was F'ing tight. i could not just press it in, i had to use the Rubber Mallet to tap it in.

I used about 7.5ish quarts. i put 7 in after doing it slowly.

I put 6 in cuz i new i could at lest put 6, Then i slowly added more after letting it warm up
and going though the gears and checking and adding.

Then after putting all 7 in, it was just at the full line, now that was week ago, yesterday i checked it again and it was down about 1/2 a quart so i added and checked,
and today just now i checked it, its sitting nicely right at full
You are counting full at the middle of the crosshatch right?
nope almost at the top when its fully warmed up.
Old 12-20-2006, 08:06 PM
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You may have a little too much fluid...not sure if it'* related to the problem though.
Old 12-20-2006, 08:07 PM
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Originally Posted by bonnie94ssei
May have a little too much fluid...not sure if it'* related to the problem though.
along that is not Above the Top line on the hash mark then it fine. and it was in the middle before and i still has having the problem
Old 12-21-2006, 07:18 AM
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Personally...You saw what happened when I used that same stinking rubber mallet on my car.

Hop down the bunny trail and get another filter kit. I'm thinking part of the plastic cracked when you tapped it. Replace...refill...
Old 12-21-2006, 07:57 AM
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Yup maybe :?

The weird thing is that this morning... it sorta worked fine, I put it into OD and it took 2 or 3 sec and it went in :?
Old 12-21-2006, 08:03 AM
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That'* not my idea of fine.

That rubber mallet isn't a friendly one.


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